diff --git a/drivers/mmc/host/sdhci-iproc.c b/drivers/mmc/host/sdhci-iproc.c
index cce390fe9cf376c13279a9d3760022ac39ecf365..032bf852397f95a3fe8aea5ee08149ee38e3c1d5 100644
--- a/drivers/mmc/host/sdhci-iproc.c
+++ b/drivers/mmc/host/sdhci-iproc.c
@@ -173,6 +173,23 @@ static unsigned int sdhci_iproc_get_max_clock(struct sdhci_host *host)
 		return pltfm_host->clock;
 }
 
+/*
+ * There is a known bug on BCM2711's SDHCI core integration where the
+ * controller will hang when the difference between the core clock and the bus
+ * clock is too great. Specifically this can be reproduced under the following
+ * conditions:
+ *
+ *  - No SD card plugged in, polling thread is running, probing cards at
+ *    100 kHz.
+ *  - BCM2711's core clock configured at 500MHz or more
+ *
+ * So we set 200kHz as the minimum clock frequency available for that SoC.
+ */
+static unsigned int sdhci_iproc_bcm2711_get_min_clock(struct sdhci_host *host)
+{
+	return 200000;
+}
+
 static const struct sdhci_ops sdhci_iproc_ops = {
 	.set_clock = sdhci_set_clock,
 	.get_max_clock = sdhci_iproc_get_max_clock,
@@ -271,6 +288,7 @@ static const struct sdhci_ops sdhci_iproc_bcm2711_ops = {
 	.set_clock = sdhci_set_clock,
 	.set_power = sdhci_set_power_and_bus_voltage,
 	.get_max_clock = sdhci_iproc_get_max_clock,
+	.get_min_clock = sdhci_iproc_bcm2711_get_min_clock,
 	.set_bus_width = sdhci_set_bus_width,
 	.reset = sdhci_reset,
 	.set_uhs_signaling = sdhci_set_uhs_signaling,